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So…what did the Civic need? While swapping tires for events, I noticed that one of the steering rack bellows was torn and wide open. That was the first item on the list…the first of many. Knowing that the rack would have to be removed to replace the bellows, I decided to replace my crumbling, 12 year old poly bushings.
Moving along…
A few seasons ago, I installed a creatively engineered catch can that involved a lot of vacuum tubing, a used MTF container. I cut the check ball out of the PCV and plugged the nipple on the intake manifold. The “hack” worked and I stopped sucking oil into the intake manifold that was sloshing into the breather canister on the back of block during very hard right hand turns. This had always intended to be a temporary fix and I decided that the permanent solution would be part of my maintenance work. With that in mind, I knew that accessing the block ports would greatly be simplified if I removed the intake manifold. Since I would be removing the manifold, I decided to install a thermal barrier gasket. I had used one in the past and wanted another. What I remembered from my past experience was that the original studs were not long enough for the nuts to be fully engaged. I found extended studs and added them to the list.
Over the past two seasons, I started to see that I was blowing smoke when decelerating from higher rpms. My 20+ year old valve seals were losing their edge. I didn’t feel the need for a full valve job and elected to replace the valve seals with the head still attached to the engine. A friend of mine found a great tool designed to make quick work of the job.
One other problem I was experiencing was oil starvation during hard right hand turns. Sadly, I do not have an oil pressure gauge to prove my experience, however noticing that VTEC was dropping during those turns was enough for me to realize that I was losing pressure. In order to avoid the issue, I had to overfill by at least a half quart of oil. I ordered a Moroso 5.5 qt. pan which includes trap doors and baffles for better oil control. When I dropped the original pan, I discovered that my oil pick-up was dented. I’ll get into more detail shortly.
Moving to the back of the car, I found that rubber in my adjustable camber links had dry rotted and needed to be replaced. They were ten years old and served their purpose. While I was working back there, I decided to replace my original compensator arms (toe links) as well as replace the poly urethane pivot bushing and lower control arm bushings. More on that shortly.
My lengthy intro aside, here is the short list of all the work I completed.
Starting on the rear suspension, I worked my way through removing most of the bolts with no issues. Years of maintaining the car, and liberal use of anti-seize, have prevented the bolts from rusting in place. Unfortunately, the inner compensator arm bolts had never been removed and required the use of a cutoff wheel. Once everything was removed, it was time to install the new bushings and arms.



For the engine block breather kit, I decided to go with a kit from B&R fittings. They were willing to assemble a “back of block” kit that didn’t include hardware to drain back to the pan. I was going to mount the can low and wouldn’t need the additional hardware. My though process for using the back of the block was that I could vent the block without having to modify my valve cover. With no fabrication required, the installation was relatively easy.










Prior to the first race, I also needed to wrap up my throttle cable replacement. The last step involved creating a proper pedal stop to prevent the cable’s rubber damper form being damaged. You can read about the work here.
At this point, the first part of the refresh project was completed. The project stepped well beyond the original scope at this point. For the most part, on a car this old, I didn’t mind having to order more parts to ensure future reliability. Parts like the oil pick-up, CV boots, fresh brakes, radiator hoses as well as several ancillary “nuts and bolts”. I had hoped that the work and expenses would drop off as I worked my way through the season. Alas, the Civic had other plans. Read about the continuing adventure in the next installment of Project Civic!
]]>Who really thinks about their throttle cables? I know it’s not on my mind. I think about how new cars don’t have them and it makes me sad. That observation aside, I noticed that my ’94 Civic (22 years old at this point) had developed slack in the cable. I had to push the pedal slightly before the engine started to respond. I knew I had set the slack properly the last time I removed the cable. I opened the hood and clearly noticed slack that wasn’t there before.
I really don’t know why or how slack would develop over time and didn’t really have the time to dig into it so I grabbed a pair of 12 mm box wrenches and adjusted the slack and everything was back to normal.
Shortly after the fix, I ran at an autocross. After my 3rd or 4th run, I noticed that I had significant slack in the cable. After finishing the rest of my runs, I headed home. Thinking the cable itself was stretching or in some way coming apart, I drove gingerly to avoid having to be towed as a result of a failure. While driving home, I tried to figure out the problem. Stretching fundamentally makes no sense. I strongly doubt I, or anyone for that matter, has enough strength to apply the pressure necessary to exceed the steel cable’s yield strength. More than likely, something on the pedal side was causing my problem.
Before I get to the actual problem, I need to disclose a detail. Several years earlier, while stripping sound deadening and other unnecessary parts from my Civic, I removed the firewall pad. The pad was thick dense foam and extended under the gas pedal. It acted as a throttle pedal stop. Without the pad, the pedal never made contact with anything when fully depressed. At the time, I didn’t think much of it and over the years, completely forgot about it.
So, what happen? The Civic and Integra throttle cable have a rubber damper on the interior side of the cable. The damper protects the throttle body and pedal assembly from over extension caused by the soft throttle pedal stop, or any number of other potential issues. Not having the foam pad to act as a throttle pedal stop subjected the damper to high levels of stress during full throttle application. I would guess that had I never removed the thick firewall pad, this damper would have lived forever. Alas, by not addressing it years ago, I finally destroyed the rubber damper and added an alarming amount of slack to the cable.

One, of many reasons, why I love autocrossing/tracking old Hondas is that parts tend to be relatively inexpensive. I was able to buy an OEM replacement from Honda Parts Unlimited for less than $30. Although the stock Civic throttle cable worked for my swap, I decided to buy the correct cable for the engine from the Integra GS-R.



The final step in this repair is to create a proper throttle pedal stop. My first idea was to use heavy rubber pads and stacking them to get the proper height. I didn’t think this would be an elegant solution to the problem and decided to search online for OEM solutions. I quickly found a possible solution by using a ’96 Honda Prelude pedal stop. Without having exact dimensions, I wasn’t sure it would work. I was able to buy a brand new one through AFHparts.com for less than $20 shipped. It was considerably bulkier than I thought it would be and it had protrusions that would allow it to be mounted through padding and carpet. Not yet defeated, I decided to see if I could make it work. Keep reading for the details.






The large hole left by modifying the pedal stop allows for fine tuning. Moving it up and down, because of the wedge shape, changes the height. With the help of my wife, holding the pedal to the floor, I was able to confirm that I was still getting full throttle.
There you have it. I have a fresh new throttle cable and a solution that will prevent a future failure of the cable damper.
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Tools Necessary
The installation process is very easy. Start by removing the spark plug wire cover. After you’ve removed the cover, pull the plug wires out and lay them over the side. Remove the valve cover and set it aside.

Following the removal of the oil rail is the removal of the cam cap next to the VTEC Solenoid. There are two more 10 mm bolts that need to be removed. Carefully pry off the cap and the original seal.
With everything out of the way, it is time to prepare the new seal. Start by coating the rubber o-rings with oil. For added protection, add a bit of sealant to the inner edge of the back side of the new seal. I have skipped this step with no leakage issues.

Reinstall the cam cap and torque the bolts to 7 ft-lbs. Next, reinstall the oil rail and torque the 12 mm bolts to 20 ft-lbs and the 10 mm bolts to 7 ft-lbs. If necessary, install new a valve cover gasket and spark plug seals then install the valve cover, spark plug wires and spark plug cover.

In my case, the motor itself was the problem causing a short that disabled both the needle movement and the odometer operation.
Before ordering any parts, test the vehicle speed sensor. The factory service manual is a good source for diagnostic information. If the sensor is in good working order, try the donor cluster to verify that it’s working properly.
These instructions will work for nearly any Nissan that uses a similar speedometer. I know that the ’95-’98 240SX used a similar design.
Tools Necessary:

After removing the screws, the speedometer can be removed.

Once you’ve removed the solder and screws, you can remove the board. Be aware that the odometer’s motor is plugged into the board.


The next step is a difficult part of the project. If you try to pull the motor off without holding the shaft, you run the risk of pulling it through and ruining the small return spring. You can try and rely on the needle holding the shaft in place, however it is a substantial risk. Use a very small set of locking or clamping pliers to hold onto the shaft.

Once you have the shaft supported, slowly pry off the motor.

Now that everything is apart and the donor parts are ready to install, you can start assembling the speedometer. I would suggest using all of the new pieces from your donor cluster.
First, install the new odometer motor.
The next part of the process is complicated. Both the shaft and the motor need to be at their “home” position which is 0 mph. Returning the motor to its home position is the hardest part. You may need to solder the motor to the circuit board, screw it into the cluster, connect the cluster and power-on the ignition. This will bring it back to the home position. If you do not do this, you could end up with a needle that will rest at something other than 0 mph when the ignition is off. Like this:

The whole process may take some trial and error but it can be accomplished.
Once you get that resolved, screw the motor in place, push on the circuit board and reinstall its screws and solder the motor pins.
Set the speedometer back into the cluster and secure it with four screws from behind.
Finally, reinstall the cluster.
Ultimately, the easiest thing to do would be to use the entire donor cluster or possibly the speedometer itself (if your donor cluster is a base model version and you want to retain your tach. If the mileage is close or you’re not worried about losing the trip meter, you could skip the hassle of soldering and properly clocking the motor to the shaft/needle.
Good Luck!
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