I’m kicking off a new series of posts with this write-up and the idea is to outline seemingly invisible parts on a car that are normally not considered normal wear items. However, a failure of one of these parts will leave you stranded on the side of the road or create a situation where safety is negatively impacted. I couldn’t really tell you at what point in a car’s life more detailed inspections are necessary. It really depends on the relative reliability of the car, the amount and nature of its use or what part of the world it is from. That being said, my first post:

Who really thinks about their throttle cables? I know it’s not on my mind. I think about how new cars don’t have them and it makes me sad. That observation aside, I noticed that my ’94 Civic (22 years old at this point) had developed slackĀ in the cable. I had to push the pedal slightly before the engine started to respond. I knew I had set the slack properly the last time I removed the cable. I opened the hood and clearly noticed slack that wasn’t there before.

I really don’t know why or how slack would develop over time and didn’t really have the time to dig into it so I grabbed a pair of 12 mm box wrenches and adjusted the slack and everything was back to normal.

Shortly after the fix, I ran at an autocross. After my 3rd or 4th run, I noticed that I had significant slack in the cable. After finishing the rest of my runs, I headed home. Thinking the cable itself was stretching or in some way coming apart, I drove gingerly to avoid having to be towed as a result of a failure. While driving home, I tried to figure out the problem. Stretching fundamentally makes no sense. I strongly doubt I, or anyone for that matter, has enough strength to apply the pressure necessary to exceed the steel cable’s yield strength. More than likely, something on the pedal side was causing my problem.

Before I get to the actual problem, I need to disclose a detail. Several years earlier, while stripping sound deadening and other unnecessary parts from my Civic, I removed the firewall pad. The pad was thick dense foam and extended under the gas pedal. It acted as a throttle pedal stop. Without the pad, the pedal never made contact with anything when fully depressed. At the time, I didn’t think much of it and over the years, completely forgot about it.

So, what happen? The Civic and Integra throttle cable have a rubber damper on the interior side of the cable. The damper protects the throttle body and pedal assembly from over extension caused by the soft throttle pedal stop, or any number of other potential issues. Not having the foam pad to act as a throttle pedal stop subjected the damper to high levels of stress during full throttle application. I would guess that had I never removed the thick firewall pad, this damper would have lived forever. Alas, by not addressing it years ago, I finally destroyed the rubber damper and added an alarming amount of slack to the cable.

As you can see, more than half of the rubber damper has crumbled away.
As you can see, more than half of the rubber damper has crumbled away.

One, of many reasons, why I love autocrossing/tracking old Hondas is that parts tend to be relatively inexpensive. I was able to buy an OEM replacement from Honda Parts Unlimited for less than $30. Although the stock Civic throttle cable worked for my swap, I decided to buy the correct cable for the engine from the Integra GS-R.

Brand new OEM Integra cable from Hondapartsunlimited.com for less than $30.
Brand new OEM Integra cable from Hondapartsunlimited.com for less than $30.
The original Civic and the Integra GS-R cables are nearly identical.
The throttle body side is virtually identical except for the "keyed" nut that helps locate the cable on the throttle cable bracket.
The throttle body side is virtually identical except for the “keyed” nut that helps locate the cable on the throttle cable bracket.

The final step in this repair is to create a proper throttle pedal stop. My first idea was to use heavy rubber pads and stacking them to get the proper height. I didn’t think this would be an elegant solution to the problem and decided to search online for OEM solutions. I quickly found a possible solution by using a ’96 Honda Prelude pedal stop. Without having exact dimensions, I wasn’t sure it would work. I was able to buy a brand new one through AFHparts.com for less than $20 shipped. It was considerably bulkier than I thought it would be and it had protrusions that would allow it to be mounted through padding and carpet. Not yet defeated, I decided to see if I could make it work. Keep reading for the details.

Here is an OEM, '96 Honda Prelude pedal stop. It's bulkier than I thought it would be but it will do the trick.
Here is an OEM, ’96 Honda Prelude pedal stop. It’s bulkier than I thought it would be but it will do the trick.
I had already started cutting it before I thought to take a picture. The top and bottom protrusions were identical. All three needed to be removed for this idea to work.
I had already started cutting it before I thought to take a picture. The top and bottom protrusions were identical. All three needed to be removed for this idea to work.
While testing fitting, I realized that I needed to cut the bottom tab to address the fact that there is a bend in the floor. This is what is left after all of the cutting and test fitting.
While testing fitting, I realized that I needed to cut the bottom tab to address the fact that there is a bend in the floor. This is what is left after all of the cutting and test fitting.
I held the stop in place and made sure the pedal made contact. I marked the hole and used a step bit to drill the hole.
I held the stop in place and made sure the pedal made contact. I marked the hole and used a step bit to drill the hole.
I used a rivet nut to create a threaded hole to mount the stop.
I used a rivet nut to create a threaded hole to mount the stop.
I used a few washers to make up for the dip in the sheet metal (behind the carpet) and bolted the stop in place.
I used a few washers to make up for the dip in the sheet metal (behind the carpet) and bolted the stop in place.

The large hole left by modifying the pedal stop allows for fine tuning. Moving it up and down, because of the wedge shape, changes the height. With the help of my wife, holding the pedal to the floor, I was able to confirm that I was still getting full throttle.

There you have it. I have a fresh new throttle cable and a solution that will prevent a future failure of the cable damper.